RUG/Pennsylvania/State College/Printers/PSU [email protected]

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Revision as of 12:18, 29 April 2012 by Mtg5072 (talk | contribs) (Build Notes)
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[email protected] is now fully operational in all axes. The next step in its developement will now be to undergo print testing, or alternatively, convert the electronics to RAMPS1.4 with Marlin Firmware now that all electrical components have been confirmed opperational.

Pennsylvania State University (PSU) [email protected] is in operational mode and continue to be in diagnostic form. Within next week, we have an idea how to approaching for the future project.

[email protected] current status

Build Notes

The majority of the initial PSU [email protected] build was completed by original owner, before it donated by after prolonged difficulties regarding its initial operation.


We were fortune enough to have all the working electronic kits and installed as instructed. Microcontroller for [email protected] model 1:Microcontroller Olimex Philip LPC-H2148 (under ARM) Apparently, we are missing the JTAG cord which is important for flashing the microcontroller. I believe we are specifically looking for OpenOCD with firmware v4. However, the board were flash for firmware v3. Firmware module


Currently, PSU [email protected] is using [email protected] v.23 made by cornell university for mendel 1 and driver [email protected] Both are externally uploaded into the computer, and communicate with the PSU [email protected]

  • Future project:
    • Convert electronics to RAMPS1.4 with Marlin firmware. This would allow [email protected] to our ultilize our RepRap slicing and control software, since original [email protected] software relies on .Fab files (developed by [email protected]), instead of standard gcode.


Currently we have Acrylic Winsor Blue available for part to print. More to come on order and check out vendors for harware and material

Diagnostic Notes

Currently, [email protected] machine has a working X axis and Z axis. Y axis does not function very well because there is something wrong with the motor not being adjusted. Also, the X axis seem to be driven itself after the program are close, which is not good. With in this week, we can expected to get the [email protected] ready for future project.

Future Projects